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134    CHAPTER 11 Nuclear reactor safety




                            The Doppler coefficient in the fuel is always negative, so fuel temperature is a
                         stabilizing effect. The power coefficient is the net effect of the negative Doppler
                         effect and the positive void reactivity effect. Since at low power levels, fuel temper-
                         ature feedback is smaller than at high power levels, the positive void effect domi-
                         nates. The RBMK has a very undesirable large positive power coefficient at
                         low power.
                            Another important safety-related feature of the RBMK reactor is the design of its
                         control rods. Insertion drives them into water-filled channels. The positive reactivity
                         associated with removal of water would be overwhelmed if the control rods con-
                         tained a strong neutron absorber along its full length. But the bottom section of
                         the control rods contains graphite, a much weaker neutron absorber than water. Con-
                         sequently, the bottom of the control rod introduces positive reactivity upon insertion.
                         The part of the control above the graphite section contains a strong neutron absorber
                         and it introduces negative reactivity when that portion enters the core.
                            The accident occurred because of problems initiated by an experiment designed
                         to evaluate the potential of a way to improve emergency cooling of the reactor. In the
                         event of a reactor scram and simultaneously losing electrical power, diesel genera-
                         tors start to provide electricity to power cooling pumps, but the rise to full generator
                         power is slow. So, the possibility of getting temporary electrical power from the tur-
                         bine as it coasted down was to be evaluated.
                            The experiment was to be performed with the reactor at a power level of 700 to
                         1000 MWth. This would have avoided the high positive power coefficient at lower
                         power levels. However, stabilizing the power level at the desired value did not occur
                         as planned. Furthermore, delays caused an operator shift change to operators who
                         were not as well informed about the test procedure.
                            Power reduction from full power began and had reached about 50% power when
                         the dispatcher prohibited further power reduction because of grid power require-
                         ments. After a delay, permission was granted to continue with power reduction.
                         In the attempt to reduce the power level to that needed for the experiment, power
                         was inadvertently reduced to a very low level (around 30 MWth). At this point
                         the operator started removing control rods to increase power. Because of Xe-135
                         buildup at low power due to I-135 decay, a number of control rods were withdrawn
                         to compensate for the reactivity loss due to Xe-135. Power eventually stabilized at
                         around 200 MWth. It was decided to proceed with the test even though the power
                         level was far below that prescribed for the test. It was a condition in which the reactor
                         had a very strong void coefficient. It was a fatal decision.
                            The steam flow to the turbine was stopped to start the test. Pumping power
                         decreased as their electrical power from the slowing turbine—generator decreased.
                         Coolant flow to the reactor decreased, boiling of coolant increased, reactivity
                         increased, and fission power increased rapidly. The increased power caused further
                         boiling and further increased reactivity. This void reactivity (along with reactivity
                         increases caused by burnout of Xe-135) caused strong reactivity feedback and con-
                         tinuing uncontrolled power increase. Because key personnel were killed and records
                         were lost, there is confusion about events that occurred at this point. It is possible that
                         an attempt to stop the power rise by inserting control rods made the problem worse
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