Page 140 - Standard Handbook Petroleum Natural Gas Engineering VOLUME2
P. 140

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 Fkw by heads, swpbbing. etc.   The 5Shaped Cum. Shut-in at   Ei'
 Them em many variations caused   surface, return of gas into 801~-   Packer failed. reset, and held.   Run away dock. Clock spring
      Remvered some mud and reservoir
                          released when tool WBS  opened.
 by avebblng. fkw by heeds, choke   tbn, small permeable zona In   fluids in reduced amount8.   Reuwery Included formation
 Plugghg. etc. Recovery hCludeS   tight llquld Wiled formath,   fluids in normal amounts.
 reservoir  fluids. Swabbing may-   etc.. glve such cum durlng build-
 cause a pmssure decline If  Huid   up. Recovery Includes reservoir
 levels am lawsred.   fluids in normal amounts.
 I
 TWI failed  IO  open.  NO fluid   Clock dld not run. Recovered   Clock stoppad on opening tool
 TWI felled to close. No bund-   excepl maybe a litlle mud is   reservoir flulds In normal   and started agah when tool
 up 1s obtained. Recovery includea   recavered. Measured pmssure   amount.   was shut in. Recovered resenroir
 brmsSon flulda   may tend to decllne to that   flulds In normal quantities.
 In the reservoir.
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 PdmrYMandmuMnot   Pedcer falled at tlme of shutln.   Uniform siii in clock   Clock stopped upon maching
                          bottom and started when started
 be mset. Recovered mud wlth   Reawered reservoir Huids in   mechanism. Tlm scale is In   mmhlg out of hole. Recovered
 some
 very llllle brmatbn fluld.   normal amounts ~JXI mud as   error. Recovered reservolr   reservoir flulds In normal
 mqulred to equalii pressure.   Nuids In normal amount&
                          quantities.
 Figure 5-63. Continued.
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