Page 191 - Advances In Productive, Safe, and Responsible Coal Mining
P. 191

170                          Advances in Productive, Safe, and Responsible Coal Mining

         (28cm), of which less than 1.5in. (3.8cm) was roof dilution meaning that OSD at
         this mine primarily consisted of floor dilution. Mining equipment in use required
         a minimum mining height of 6.0ft (1.8m) giving opportunity to reduce dilution
         by 6.4in. (16.3cm).
            With these data in hand, the project team established a goal to reduce dilution by
         3.0in. (7.6cm) as a first step with the expectation that as mine personnel became
         comfortable working in slightly lower mining heights, further reductions may be
         attempted. In establishing this goal, it was noted that it had been achieved 8%–12%
         of the time during the phase 1 data collection period as indicated in Fig. 9.4.This further
         supported the feasibility of consciously reducing dilution to achieve the established
         goals.
            Using data collected in phase 1 coupled with engineering design modeling, an OSD
         educational awareness program (EAP) was prepared. The program included
         computer-generated models showing out-of-seam mining levels, the influence that
         existing OSD levels had on product quality, and the associated economic impact that
         resulted. The program also set forth the OSD reduction goal and explained the effect
         that achieving it would have on productivity and profitability. Chugh’s research team
         presented the EAP to a mine management team who then delivered it to continuous
         miner and roof bolter operators working on the mechanized mining unit being
         evaluated.
            Immediately following presentation of the EAP, a second phase of data collection
         commenced. Phase 2 data collection lasted 2weeks during which time study data
         were collected for another 30 cuts and out-of-seam dimensions were measured at
         275 locations while the same 11-entry section advanced four more crosscuts. These
         data were analyzed to determine any productivity improvements and OSD
         reductions.
            Time study results indicated a marginal increase in loading time (38s per haulage
         unit in phase 2 as compared with 37s per haulage unit in phase 1). This difference is
         not statistically significant at a 95% confidence interval, so it cannot be scientifically
         concluded that the educational program resulted in any measurable productivity
         improvements. However, researchers believe the difference is a result of the cautious
         approach adopted by continuous miner operators in attempting to stay in-seam and
         reduce OSD. Earlier studies [1, 18] conducted by some of the same research team
         members showed that longer loading times result in greater utilization of haulage unit
         capacity, which is the single biggest productivity factor in continuous miner batch
         haulage systems.
            Fig. 9.5 shows the progression of mining heights and dilution from just prior to
         presentation of the OSD EAP through 2weeks of phase 2 data collection. The center
         of the coal seam is represented by the y-coordinate of 0ft. Red, blue, and violet
         colors represent mined thicknesses of roof, coal, and floor, respectively. The figure
         indicates a consistent post-EAP reduction in roof dilution; however, floor dilution,
         although reduced immediately following the EAP, drifted back to and even beyond
         pre-EAP levels over the 2-week phase 2 data collection period. It should be noted
         that lithologic properties of the geologic cross section at the study location enabled
         easier detection of the coal-roof interface whereas the coal-floor interface was not as
         apparent.
   186   187   188   189   190   191   192   193   194   195   196