Page 413 - The Toyota Way Fieldbook
P. 413

386                       THE TOYOTA WAY FIELDBOOK


            Many people look at this A3 and immediately think that it is “too busy” or
        “complicated.” This is a normal reaction to a very involved A3. There is a lot of
        information fit into a small space. If this A3 were presented to you, you would
        see that in fact the entire story can be explained in about three and a half min-
        utes and is quite clear. The following text would be used to explain this A3, and
        it is presented as a reporting of results (the activity is complete):

            As you can see [pointing to the trend graph in “Define the Problem Situation”], the
            fabrication line was consistently below goal for units per hour, and at the end of last
            year it had gotten worse. As a result of being under the units per hour goal [point
            to the overtime graph] there was approximately $80,000 per month in overtime
            cost, which was increasing, and also our late shipments to the customers [point to
            the late shipments graph] were increasing. If we did not take action, this problem
            most likely would have gotten worse. [End of the Problem Situation section.]
                An analysis of our production losses [point to the first graph in “Problem
            Analysis”] showed that we were losing time during the operation cycle, and our
            available run time was reduced because of cleaning time. We were spending 30
            minutes per shift for cleaning and wanted to reduce that to 15 minutes per shift
            [point to the chart]. Observation of the work area showed that contaminants were
            not being contained properly, causing additional cleaning time. Reducing the
            cleaning time by 15 minutes per shift will increase the units per hour by 2.5.
                Observation and analysis of the work steps indicated 10 seconds of walking
            time for this operation [point to the yamazumi, or stack chart]. The worker flow dia-
            gram [point to the diagram] shows that the location of parts and equipment was
            causing excessive walking time. A reduction of one-half of the walking will be a
            five-second savings per cycle, which will yield an additional seven units per labor
            hour. [End of the Problem Analysis section.]
                To get some temporary relief from this problem we decided to perform cleaning
            during lunch and breaks [point to each countermeasure in the “Action Plans to
            Correct Problems” as it is mentioned]. We had a temporary cleaning service that
            performed that task until we could implement the permanent countermeasure to
            more effectively collect the dirt. Also, we taped cardboard boxes to certain locations
            on the machine to capture dirt temporarily. This made the clean-up easier. These
            short-term countermeasures were completed immediately. During the second
            week we changed the layout of the work area and repositioned the start button.
            These changes reduced walking time and reduced the cycle time. Our permanent
            countermeasure was to enclose the bottom of each machine with a skirt to further
            reduce the cleaning requirement.
                We needed to make some modifications to the dust collection system, and
            each machine was modified as well. This task required the support of maintenance
            and engineering, and we planned to complete one machine per week over a four
            week period. We checked progress each week to make sure we were on target.
            These are permanent countermeasures that will reduce the cleaning requirement
            to 15 minutes. [End of the Action Plans to Correct Problems section.]
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