Page 203 - Failure Analysis Case Studies II
P. 203

188
          was undertaking its 1286th pressurized flight in addition to 255 flights without cabin pressurization.
          The Court of Inquiry [l] concurred with the findings of the RAE investigation [2] that the cause of
          the accident was sudden cabin failure due to fatigue crack growth followed by the break-up of the
          aircraft. The accident which occurred to G-ALYY was attributed  to the same cause, as the flight
          circumstances were similar, although insufficient wreckage was ever recovered to prove the case.
            The root of this rapid failure due to metal fatigue was shown to be high stresses around cut-outs,
          such as windows, in the aircraft skin. The aircraft manufacturer, de Havilland, had made estimates
          of these stresses averaged over a large area, and ascertained the fatigue life of the aircraft by testing
          sections of the cabin and the 22 gauge (0.71 mm) pressure cabin skin was thickened  to 20 gauge
          (0.91 mm)  around the windows. However,  the Court of  Inquiry  reported  that the nature of  the
          sections used meant that they were not representative  of  a whole aircraft,  as bulkheads fitted to
          these sections to enable pressurization  may have affected the stresses around the cut-outs in the
          locality. This enabled the forward cabin section tested by de Havilland to withstand  18,000 cycles
          before fatigue failure from a defect in the skin near the corner of a window. In addition, this section
          was proof  tested to  16.5psi (114kPa), or twice the operating pressure, before the fatigue testing
          began, and this may have caused local plastic deformation in the regions of high stress of interest
          here [l]. Proof  testing of the pressure cabin was undertaken  on all Comets during manufacture,
          before acceptance  by  BOAC, and at predetermined  times during  service, to  11 psi (76 kPa), but
          never to  16.5psi (114kPa),  and a safety valve to prevent  overpressurization  of  the cabin during
          service was set to 8.5 psi (59 kPa).
            Cracks were known to be present in the aircraft upon manufacture, and there was an approved
          technique for identifying such defects and “locating” them by drilling the end of the crack with a
          & in. (1.6mm) drill [l]. In most cases, the crack was seen not to extend beyond the location hole,
          and this was assumed to be adequate security against further crack growth. In fact, there was a
          “located” crack near the forward port corner of the rear ADF (automatic direction finding) window
          (Fig. 3) on Yoke Peter, which did not grow beyond the locating hole until the final failure of the
          cabin.
            The failure of Yoke Peter was deduced to be a fatigue crack near the starboard rear corner of the
          rear ADF window (Fig. 4). This crack emanated from a lOmm diameter bolthole, and propagated
          to failure after unexpectedly few pressure cycles of the cabin. This bolthole in such a highly stressed
































              Fig. 4.  Close-up views of the Failure in the skin of Comet G-ALYP. Crown Copyright. Reproduced with the
              permission of the Controller of HMSO.
   198   199   200   201   202   203   204   205   206   207   208