Page 262 - Membranes for Industrial Wastewater Recovery and Re-Use
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Case studies  231















                          (a)                             (b)
                  Figure 5.2  (a) Microfiltrationmd (b) reverseosmosispilotplnntsat Flag Fcn



         3.7 for suspended solids and 3.3 for BODj. Smaller variations are observed for
         COD  (2.2) and  total  phosphorus  (1.5). Seasonal  variations  occur  due  to  a
         vegetable  processing  factory that discharges  effluent  of  very  different  quality
         depending on the food being processed.
           The permeate quality from both membrane plants was both reliable and in line
         with previous values found from pilot plant work. Feed quality to the RO plant
         can show large variation with rainfall: for instance, a conductivity of between
         800 and 1200 pS cm-'.  Permeate  quality from the RO plant is  38.5 pS cm-'
         representing  a  rejection  of  96.7% on  average.  Overall  rejection  of  TDS  is
         93% with specific rejections of  sodium and calcium of  95 and 99% respectively
         (Table 5.20).
           The main issue of  concern was membrane fouling reducing output from the
         MF plant  and increasing  pressure  on the feed stream of  the RO plant. Initial
         operation of the plant showed excellent water quality but high RO fouling rates.
         The RO feed pressure increased at a rate of  1 bar per hour at worst due to rapid
         build up of  calcium phosphate. Changes to upstream operation has effectively
         controlled the problem and membrane cleaning is now required every 6 months
         on average.
           The Flag Fen plant is currently operating well and exceeding the target water
         qualities  set  down  in  the original  negotiations.  The quality of  the delivered
         water has enabled ultrapure water production at the power station to increase
         by 20%. Coupled to this is a reduction of over 90% in the costs of ion exchange
         regeneration  due  to  an  increase  in  the  operating  cycle  of  the  twin  bed
         demineralisation plant from 8 to 60 hours. Overall, 12 50 m3 of tap water per day
         have been saved which has reduced the station's total water use by 11%. Client
         receptivity to the scheme is very high as supply is guaranteed and operating costs
         decreased. The high-purity  water plant cost around €1 000 000 ($1 524 000)
         and each membrane stage has an operating cost of  7.5~ m-3 ($0.11 m-3). The
         success of  the scheme has attracted media attention and the project has won a
         number  of  prestigious  awards  including  the  2  000  Water  UK/Environment
         Agency  water, the 2001  IChemE innovation efficiency award and the 2001
         Green apple award.
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