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Ethylene pipeline  cleaning


      encountered, attributable to the restrictive tees. A summary of the inspection
      runs is presented  in Fig.6.

        Recommissioning


        Pipeline recommissioning commenced on day 24. Pigging was  complete
      on 20th May, leaving 8 days for leak checking and maintenance work. On day
      23, the pipeline pressure  was increased  to  2300kPa (330psi), and ethylene
     vapour was introduced  at  23,000kg/hr. Venting took  place at BV10 (north
      end) to maintain pressure in the pipeline. The vent stream was analyzed by
     portable gas chromatograph to detect the ethylene/nitrogen interface. It took
      28 hours for the interface to reach the north end of the pipeline. At this point,
      the vent stream was flared until product-quality ethylene was detected. This
      took  an additional four  hours.  Flaring was then  stopped  and  the  line was
     allowed to pressure-up to operating pressures. The pipeline was put back into
      service on  12th June, 30 days after  shutdown  operations  began.




        PROJECT RESULTS


        Pipeline capacity


        Calculations from pressure-drop readings taken after the pipeline was put
     back into service  revealed that the  pipeline capacity had been  restored  to
      I60,000kg/hr  (an  increase  of  26%). This was  confirmed in  August, when
     pipeline flows reached  157,000kg/hr without  maximum operating  pressure
     limits  being  exceeded.  Fig.7  lists  friction  factor  ratios  before  and  after
     cleaning.


        Pipeline integrity


        Results from  the  inspection  revealed  only five  reportable defects  (more
     than  20% metal  loss)  along  the  entire  180-km  (110-mile)  pipeline.  The
     maximum    depth  reported  was  34% metal  loss.  Novacorp  performed  an
     engineering critical assessment on the data, and determined that no immedi-
     ate  repairs were  required.  AGEC  will  excavate,  inspect  and  recoat  these
     defects over the next two years.


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