Page 436 - Boiler_Operators_Handbook,_Second_Edition
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Controls                                                                                            421


               to open it. Of course there were times when we forgot  pumps in operation to determine when recirculation is
               to open an isolating valve on that recirculating line too!  necessary and open a solenoid valve in the recirculating
               Why, I don’t know, because we should have left them  line when necessary. I made it a point to have the sole-
               open.                                                noid valves supplied as normally open and the controls
                    Another feature of those recirculating lines that I  energize it to close. That way it will fail to recirculating
               used in later designs was combining all the recirculat-  to prevent damage to the pump. You should still use
               ing lines into one line returning to the deaerator with  orifices but they can be a little larger.
               another orifice (sized for all pumps) so some of the recir-
               culating water would flow backwards through the other,  Goofy Controls
               idle, pumps to keep them warm (the recirc line was con-     The advent of microprocessor controls allows us to
               nected before the discharge check valve). Knowing what  add more and more features to a control system. I like to
               I now know about the effect of piping stress on pumps  think of them as ways to help the boiler operator. There
               (see piping flexibility) I think it also prevented damage  are, however, some features added that make it more
               to the pumps.                                        difficult for the operator.
                    During work on a problem with some boiler feed      I’ve encountered some fairly stupid concepts in re-
               pumps in 1999 I also discovered that higher pressure  cent years. Not because they were dangerous or wrong,
               boilers require so much feed pump energy that the recir-  they just made life difficult for the operator. One I ran
               culating flow represented a significant amount of extra  into involved a boiler control system where the designer
               horsepower and, more importantly for that particular  decided that any time any variable got out of range
               customer, a significant reduction in the amount of water  (more than 100% or lower than zero) all the controllers
               that could be supplied to the boiler.                should switch to manual. With that logic, on a balanced
                    Plants operating at pressures of 250 psig and high-  draft boiler, every time the boiler was started and the
               er have had a solution for this problem for many years,  purge commenced all the controls switched to manual
               it’s a self contained check and recirculation valve which  because the boiler outlet dampers couldn’t close down
               consists of a spring loaded check valve that checks the  enough to prevent the furnace pressure dropping below
               main fluid flow and an integral recirculating valve that  the low end of the furnace pressure transmitter’s range
               opens as the main flow decreases. The problem with  so everything switched to manual. The boiler hung up
               those valves is they are very expensive and most plant  in manual until the operator switched everything back
               owners scream at the cost, they can cost almost as much  to automatic. Even though I explained what was hap-
               as the pump! Regardless, they work and they pay for  pening and that there was no need to switch controls
               themselves in power savings.                         to manual simply because the measured variable was
                    There is another solution that I haven’t had an  out of range the designer insisted that his system had
               opportunity to try yet and I hope to compare to those  to work that way. Hopefully it was finally resolved but
               expensive recirculating valves. The cost of controls has  I wouldn’t be surprised to visit that plant and watch the
               dropped so much I believe you can justify installing two  operators switching all the controls back to automatic
               temperature sensors on the pump, one in the suction  after every start-up.
               piping and one that senses the liquid near the pump      I also recently had a situation where a technician
               discharge (without interfering with the flow patterns)  insisted the drum level transmitter had to be set where
               to detect a rise in the fluid temperature in the pump. It  mid range was the center of the drum. There are very
               would control a small pneumatic valve in the recirculat-  few boilers out there which have a normal water level
               ing line. As long as the temperature differential is low  at the center of the drum, most are lower by two to four
               enough there’s no need to recirculate water. It eliminates  inches. I finally had to insist that the middle of the range
               the pressure loss attributable to the spring on the auto-  was at the center of the gage glass, that it had been that
               matic recirculating valve check and, by using tempera-  way for ages, and he had better set it there if he wanted
               ture differential, is oblivious to any changes in deaerator  to get paid.
               pressure that would change the temperature at which      On a recent excursion to California to look at a sys-
               steam would start to form.                           tem that had nothing to do with a boiler other than use
                    Another system I am trying is using the integrated  steam I got frustrated with the programmable controller
               controllers of automation systems to create a feedwater  logic. It prevented starting a pump while the water level
               flow calculation based on the control signals to all the  in a tank was high. It was high because the pump had
               feedwater control valves in the plant and the number of  been shut off! I had to drain the tank to get the pump
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