Page 161 - Failure Analysis Case Studies II
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            Since the piston rods were welded semi-automatically with a stationary electrode and a rotating
          work  piece,  it  was suggested that applying a gas flame for two  revolutions would  suffice as an
          intermediate  solution.  Induction  heating was recommended as the long term solution,  since the
          temperature profile will be more even through the thickness of the joint, the temperature of the weld
          joint is raised to the preheat temperature without overheating and oxidising the surface, and it is
           faster than flame heating.
            Weld penetration  was improved by increasing the current by 20% and reversing the polarity to
           electrode negative (DC current) for maximum depth to width ratio.

           6.4. General
            The above recommendations were intended specifically to remedy the problems with the weld
           failures. During the investigation a number of other areas that required attention came to light.
           0 En9  is  a  hardenable  steel but  the  hardenability  properties  were  not  being  used-instead,   the
            weldability was reduced. Steels with similar strengths but lower carbon equivalents and thus better
            welding properties and lower preheat  temperatures  needed  to be considered. Alternatively, by
            quenching and tempering the rods,  higher strengths can  be  achieved and thus a reduced wall
            thickness might suffice, resulting in lighter components.
           0 The refractory compound  shielding on the adapter that was intended to prevent carburising of
            the area that is to be welded was found to be unsatisfactory. Possible alternatives included copper
            plating and removal of the carburised area by machining. However, if the copper plating is not
            removed, this could lead to weld contamination.
           0 Much of the effect of carburising was cancelled by the nitriding process, Le., the hardness of the
            case was reduced from the specified 60 HRc after carburising to f 40 HRc after nitriding. Since
            nitriding was a major contributor to the failure, the value of this process needed to be critically
            evaluated.


                                          7.  SUMMARY
            The problem of the failed actuator piston rods was analysed and solved, the solution tested and
           successfully implemented into the large scale production of the actuators within two weeks.  No
           further weld fractures were reported.
            A large number of metallurgical aspects of the weld was considered in this investigation, most of
           which were not  profound  revelations to anyone versed in materials  science and did  not require
           exotic testing facilities or specialised expertise. The main point that the authors wish to emphasise,
           with this investigation serving as an example, is that careful consideration should be given to every
           stage of a design, processing or material selection change in any product. Too often, metallurgical
           aspects of such changes are ignored or glossed over, each change eroding the “metallurgical safety
           factor” until the sum of the changes results in a non-viable component that enters service flawed or
           has marginal mechanical properties.
            Any one of the changes outlined in Table  1 would not in itself have resulted in the failures, but
           their implementation  left fewer options and  less room  for error  for the following changes. For
           example, changing the surface treatment (based, at the time, on the customer’s colour preferences
           rather than corrosion or wear properties) raised the processing temperature from 70°C (phosphating)
           to 580°C (nitriding) which had far-reaching effects on tempering, precipitation of carbides and other
           brittle phases, residual stresses, etc. but may have proved insignificant if the base material had had
           a lower carbon content or a low carbon/low alloy filler metal had been utilised.
            This is where a well managed and frequently examined change management system such an IS0
           can play a vital role in guaranteeing ongoing unwavering quality in the face of changing suppliers,
           process  capabilities  and  customer  requirements-but   not  without  the  watchful  guidance  of  a
           materials engineer.
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