Page 46 - Handbook of Materials Failure Analysis
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3 Case Studies      39




                  3. During potentiostatic scan, the line pipe specimen did not attain passivity due to
                     high chloride level in spent caustic solution compared to water.
                  4. The rate of penetration due to pitting was increased with time as perforation.

                  3.1.8 Recommendations
                  On the basis of visual, metallurgical, design consideration, and electrochemical test-
                  ing results it was suggested to replace 1.5-in. CFL400 pipe with 4-in. diameter pipe to
                  eliminate the velocity-reduction effect in the horizontal line pipe which could also
                  prevent the formation of stagnant layer and hence the deposition of suspended solids.
                  In a continuous flow situation, the formation of local cells will be restricted by the
                  elimination of differential aeration cells.

                  3.2 FAILURE OF PLATE HEAT EXCHANGER DUE TO PITTING
                  Reprinted from Deen et al. [15]. Copyright 2010, with permission from Elsevier.

                  3.2.1 Background
                  The heat-exchanger plates failed due to pitting and perforation. This plate-type heat
                  exchanger was the part of a power generation system and it was designed to transport
                  heat of close-circuit jacket, primary cooling system auxiliary water by cooling with
                  open-circuit cooling tower (CT) water (secondary cooling system) to decrease the
                  temperature by 20 °C. Almost 32 plates were perforated by the secondary cooling
                  water in the open-circuit side of CT system.
                     In the jacket water side, the plates were arranged sequentially in two pairs, each
                  having two plates one for jacket water and the other two plates for CT water; thus, 24
                  plates were tightened in a bundle. There was similar arrangement in the auxiliary
                  water side of heat exchanger. The hot and cooling water flow arrangement is shown
                  schematically in Figure 2.7.
                     Internal lube oil and cylinder head jackets of the power engine were cooled by
                  auxiliary water and jacket water heat exchanger in a close circuit, respectively.
                     For efficient release of heat from the four power engines and maintaining the
                  appropriate temperature, each was connected with an individual CT having capacity
                  50 tons/h (Table 2.5).

                  3.2.2 Analytical Approach
                  To investigate the reason of perforation and pitting of plate heat exchanger, the
                  following procedure was adopted:
                  1. Collection of historical, design, and operational data
                  2. Visual inspection
                  3. Metallurgical analysis
                  4. Chemical analysis of every water system (raw water, reverse osmosis (R/O)
                     water, CT feed, and CT bleed water)
                  5. Investigating the electrochemical behavior of heat exchanger plates in water
                     systems
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