Page 295 - Membranes for Industrial Wastewater Recovery and Re-Use
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264  ivembranes for lndiistrial  Wnstrwatrr Rrcowrg iind Re-nsc

                                                      Fresh Dl water
                                                          I




           Polluted                                                Permeate
           nnse wat                                                to nnsing bath
             Acid




                    Concentrate back
                    to E-coat bath
                    Figiirr  5.2 3  Procrssflowdiagram ofpostpaint  water recycling systrrn


        plant results in a membrane replacement life of over 3 years. Membrane integrity
        is  checked  during  both  manufacture  and  operation.  During  manufacture
        membrane quality is monitored using air permeability  tests. During operation,
        permeate quality is monitored by a combination of visual inspection and on-line
        turbidity meters. Any individual permeate tubes seen to be passing retentate are
        removed from the collector and diverted back to the treatment tank and so there
        is no need to make interventions for incidental damage.


        5.10.3 Performance
        The plant  operates within the required  specifications for recycling  water and
        recovering paint. The main operational concern with the system is the stability
        of the paint solids which would otherwise coat the membrane, a problem which
        is controlled by pH adjustment. Bacteria contamination is also a problem due to
        the close contact of  the rinse water with air. Growth is controlled through the
        use  of  paint-compatible  biocide,  but  ultimately  the  membranes  may  need
        mechanically cleaning by hand.
          The high water demand of the process and the ability to recover valuable paint
        make the recycling scheme very favourable economically. The plant reduces the
        requirement for water and effluent treatment by  60  000 m3 y-'  resulting  in a
        €327000  ($326 146) saving. Some 18 600 kg y-l  of  paint are also recovered
        representing  22% of  the  total  annual  saving  accrued  from  the  plant.  The
        remaining saving are in labour costs associated with having to clean the rinse
        water tank less regularly. The major cost of running the plant is energy to run
        the pumps and cooling circuit which equates to a total annual energy demand of
        324000  kWh.  The  remaining  costs  are  due  to  membrane  cleaning  and
        replacement resulting in a total opex of €0.36  m-3 ($0.355  rnp3). The plant cost
        a capital  outlay of  €270000  ($269  000) with a  further €24000  ($23 600)
        required  for  first  year  financing.  The  annual  net  cash  flow  is  €435 000
        ($433 900) resulting in a pay back period of less than 8 months. Although the
        economic success  of  the plant is country-specific  a  similar  scheme in the IJK
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